Second one of the month today and we picked up right where we left off. We got the jist of everything again and re familiarized ourselves with ROBOTIC, the program we use to code our robot. We set up some challenges for our robot to accomplish. We may have not achieved them all, but we were close. We have have taken a small step backwards however, as when configuring the joystick, we lost the connection between the joystick and robot!
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Today we tried to configer and recalibrate the robot and remote.
We then messed up the controls and now it will not move using remote.
Next session we will try to fix the problems we have accumulated and done.
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